My old trustworthy 1994 txrs 200 hp lost a cylinder today after many years and many hours of faithful service . Went into a partially seized moment after dropping the cylinder. Got good compression on the remaining 5 and 0 on that one. Bolt removal looks like it will be the issue...soooo.... what happenened and what to do. All 6 plugs look perfect. 80 n sunny.
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Partially seized could be from fragments of rings/pistons - started out as larger fragments, then got chewed up and spit out.
Pull the plug and stick a scope in there.2000 Yamaha OX66 250HP SX250TXRY 61AX103847T
1982 Grady Weekender/Offshore (removed stern drive & modded to be an OB)
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Just got the boat on the lift a couple of hours ago. Water jacket part of the head came off easy, but head bolts are gonna need some heat at best.
When I spin it up, not hearing air escaping and plug on that cylinder looks perfect. Will put the torch to it tomorrow . Got limited tools and resources where I'm at.
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Salt water. And looks rough under the hood. Seeing the plugs look so perfect, maybe the oil pump failed? Not looking to be drilling n tapping for the next week or 2.
Would like to replace with something similar that I could make use of my lower unit and other parts. I'm sure pulling the power head would be a beast. Like said....got limited tools and resources here
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Originally posted by scofflaw View PostSalt water. And looks rough under the hood. Seeing the plugs look so perfect, maybe the oil pump failed? Not looking to be drilling n tapping for the next week or 2.
Would like to replace with something similar that I could make use of my lower unit and other parts. I'm sure pulling the power head would be a beast. Like said....got limited tools and resources here
How good would that be!....Try to find a similar freshwater motor....
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Originally posted by scofflaw View PostMy old trustworthy 1994 txrs 200 hp lost a cylinder today after many years and many hours of faithful service . Went into a partially seized moment after dropping the cylinder. Got good compression on the remaining 5 and 0 on that one. Bolt removal looks like it will be the issue...soooo.... what happenened and what to do. All 6 plugs look perfect. 80 n sunny.
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