Out from stator, 140v and 180 volt. Good spark on all plugs, and misfire...
Guess what, checked timing again, suddenly very wrong!
Clipped the woodruff key on the crankshaft to the magnet rotor, get a new key tomorrow, guess all is ok. For now... Trying again tomorrow when i get a new one.
Guess what, checked timing again, suddenly very wrong!
Clipped the woodruff key on the crankshaft to the magnet rotor, get a new key tomorrow, guess all is ok. For now... Trying again tomorrow when i get a new one.
Comment